Spring Update

Spring is one of my favourite times of year. Traditionally Spring has been a time for ‘new life’ and new ‘beginnings’. I’d say that 41001 is in the Spring of its life and this has recently been hit home with us as we see yet more and more progress with the project bringing it ever closer to its return to working order.

 We left you last time with the cubicle out of the power car and some sundry mechanical items left to complete. We haven’t been resting on our laurels and substantial work has been on-going with electrics and other odds and sods.

 Tony has been very hard at work with the cubicle over the past few months. We left you last time with the cubicle painted but completely bare, with most of the relays and contactors overhauled but not mounted. In the past 3 months the cubicle has gone from a bare shell to having all its relays and contactors fitted. Fitting these isn’t as easy as you’d think as we weren’t going back to what was in 41001 when we got it; the power car had this hybrid wiring that was part original prototype and part production HST. We have taken the decision to make 41001 as close to a production power car as possible to ease troubleshooting in the future. So Tony has now fitted the relays as per a production power car; this has added some relays into the cubicle and deleted some contactors – as an example, the start circuit used to have a Start Circuit Contactor (SCC) which was enormous (same size as the Lub Pump and Fuel Pump contactors). On the production they obviously realised this was overkill and replaced it with the Start Circuit Relay (SCR) which we have now done on 41001’s cubicle. With all the relays and contactors in position, Tony could start the mammoth task of wiring the cubicle. This isn’t particularly complicated, even by Tony’s own admission, but it is time consuming and requires a great deal of patience and dexterity. All our wiring is being done using railway standard approved cabling (TDE/76/P/16) which is lovely stuff to work with, being easy to strip and make off to ring crimps, but it is ferociously expensive. We managed to get the first 1000m (yes, 1km) of cable for a discounted price but having just ordered the second 1km, I can tell you those discounts don’t last! Every cable in the cubicle has a number; a simple system that BR used which means you can always work out what a cable does by looking at the ident on the cable next to the crimp, which is useful given all the cable is grey in colour! Tony has a point to point spread sheet we follow that says which two points within the cubicle the wires go between. Most of the regular crew at Neville Hill have had a go being Tony’s wiring mate and one soon gets into the rhythm of wire number being called out followed by start and end point and then working out what the neatest way of getting the cable between those two points will be. We have strategically placed loose cable ties around the cubicle frame so we can bundle together the loom as it starts to fill out. 

Tony working on the cubicle (c) John Zabernik

Tony working on the cubicle (c) John Zabernik

The cubicle is rather clever in the way it is wired – something all BR locos have had – where the control and monitoring connections come into a compartment at the top and are “made off” to a series of ring terminal posts. That means you can remove the cubicle by “just” undoing these connections and then lifting the cubicle out. There is one caveat to that, which are the heavy duty connections which come in the bottom on 41001, namely for alternator and traction. This is an area we need to look at as there is some confusion as to how 41001 has been wired up; our original documentation from 1972 shows the traction motors in a 1+4 / 2+3 configuration with the armature connections next to each other and the field connections at one end. The production cars are in a 1+2 / 3+4 configuration with armature/field/field/armature connections. This will require some more digging to see what is what with the big cables and bus-bars appearing out of the floor where the cubicle sits.

Tony has also replaced the electronics rack that was in the prototype cubicle with one kindly donated to the project by HST supremo Dave Moore at Brush. It is actually from a Class 56 but we have modified it so it fits into the prototype cubicle and also takes HST production control cards – the same as those still being used by FGW. There was a bit of metal cutting and welding required by EMT to get the rack to fit, as one of the bracing struts was just where we didn’t want it. We have also replaced the 3 phase ac short circuiter with a dc machine that was originally from 56090! The AC short circuiters were renowned for causing more fires than they prevented and the DC variety is now standard equipment on all production power cars. The short circuiter has now been mounted on top of the cubicle as per the production power cars.

41001s Electrical Cubicle (c) Tony Shaw

41001s Electrical Cubicle (c) Tony Shaw

On the power car itself a lot of work has been carried out in addition to the cubicle work. Led by James, the team have worked their way round the inside of the power car and painted all the surfaces that can be painted to provide some corrosion protection, as well as protection from oil and fuel that will undoubtedly coat the engine room floor after a few months of operation! An important area that required painting were the battery boxes underneath the power car, as these hadn’t been looked at for over 30 years. John Zabernik and Chris Rose did a very thorough strip and rub down of the internal surfaces of the battery boxes and then John Zab came armed with masks, gloves and brushes and painted the entire inside of the boxes in a special rubberised white paint, which acts to protect the boxes as well as providing a safety layer against any possible short circuits that could occur with the batteries. A very satisfying result I am sure you’ll agree. We also painted the surfaces in the cab area to ensure these were all the correct colour; the NRM had used an odd shade of grey that wasn’t as it should be so we now have it all as near to the correct “BR Grey” as we can. 

John Zabernik working on stripping down the battery boxes (c) Dan Webster

John Zabernik working on stripping down the battery boxes (c) Dan Webster

Ben, James and Gary spent a lot of time working out some of the remaining wiring in the power car. They were puzzled by the connections coming from the battery box and battery isolating switch (BIS) area, so armed with a multimeter and many pairs of hands they worked their way round each wire to see what was what. Part of this task involved ripping out the inspection lamp connections which are never used on the production power cars and they just make life more confusing for us. Once that wiring was out of the way we made good headway and managed to label all the connections as well as Ben re-wiring the BIS so that when it is in the “isolate” position it does actually isolate everything except the lights.

Ben and Gary tackled a problem that had been bothering us for some time with regard to the governor wiring; 41001 had a bit of a bodge when modified to run a governor with LDVT, instead of the original “traditional” vane motor – they put the LDVT box on the A side and the rest of the governor wiring in a box on B side. We wanted it all in one spot as per the production cars, so the A side box was removed with a view to getting everything in the B side box. However, when Ben and Gary totted up the cables in the new box they realised they were one short! So they took the bold decision to re-run the cables in some new trunking back to the front bulkhead junction box. This was relatively straight forward using some trunking that Garys company had “thrown out” during a recent move. However, they made a slight mistake and forgot to put screened cable in for the LDVT connections, so this will have to be re-done during our next visit.  

Gary working on the wiring (c) Tony Shaw

Gary working on the wiring (c) Tony Shaw

Ben and Gary also worked on putting new cabling into the front cab which went well. The cab wiring was a bit of a hit and miss affair and given the state of the heater/blower unit we removed in the autumn, we thought it best to re-wire it to avoid any accidents! The wiring isn’t too difficult, although getting the wires down a narrow gap in between the cab and bulkhead can cause some swearing and pinched fingers. We have about 75% of the wiring through now, sticking out through holes in the desk where the instruments go. We should complete this fairly swiftly once the cab lighting switch panel is re-installed. One area that is a mystery is the brake controller handle which has 9 connections, none of which are marked or documented at either the brake controller handle end or on the E70. This may require some trial and error to get it working properly.

Cab Wires

41001 cab during the full rewire (c) James Trebinski

Steve and Bob took up our main mechanical challenge this period which was to install our newly converted carden shaft into 41001. This was quite involved, as you may recall S508 has a Vulkan coupling with M16 holes, as per production, but the flange on the ZZ gearbox on the Marston in 41001 has M14 holes. So Tony and Gary had been to our storage facility one Saturday and remove a flange from one of our mountain of production gearboxes which did have M16 holes. Steve and Bob used a pulled to remove the flange off 41001’s gearbox, which was much easier than the production one as someone had put some grease on it! Then the production flange was installed onto the shaft ready to take our especially lengthened production shaft, which is a thing of beauty and looks like new! The shaft went in with a bit of swearing and all that remains is to fabricate a cover to protect those in the engine room when the engine is running from falling onto the rotating shaft.

S508 & 41001s Cardan shaft including newly fitted cover (c) James Trebinski

S508 & 41001s Cardan shaft including newly fitted cover (c) James Trebinski

So another lengthy update and hope you’ve all made this far. We have had several discussions between ourselves recently and we think its amazing how much we have achieved in a year.

Plenty more work been done…

In this update we’d like to highlight the work being done on 41001s electrical cubicle. Last time we updated you on progress 41001 had its shiny newly overhauled valenta engine sat inside mated with the alternator. So since then what have we been up to?

Well not long after we started the major work the cubicle and all associated wiring was removed from 41001. Our ‘Mr Cubicle’ Tony Shaw has been working very hard over the past 6 months or so on the cubicle both at Neville Hill and in his workshop at home. We quickly came to the conclusion that the cubicle would need a full strip down and rebuild as corrosion had occurred where water had ‘got inside’. Tony has been overhauling the relays and contactors for the cubicle in his workshop using the existing ones removed from the cubicle and utilising the spares that Valenta Diesels Limited has acquired over the years and have held in storage. All the parts have been tested and are in excellent condition meaning they are in the process of being introduced to the cubicle.

 

A view of the cubicle part way through overhaul (c) Tony Shaw

A view of the cubicle part way through overhaul (c) Tony Shaw

One of the costlier parts of this segment in the project is without doubt the actual wire itself. All the wiring in the cubicle has been removed and replaced with new wire whilst new wiring has also been installed running from the cubicle into the cab. We took this decision as whilst Tony was stripping the wiring and assessing it all he found many random wires seeming redundant with no visible purpose or cohesion, many of which were just taped up when removed in the past. The new wiring used is to the relevant railway specification and is called “Polyrad”, which seems to roughly translate as “bloomin’ expensive”! It is oil resistant and heat resistant to a point, plus its much thinner than the original – the insulation is thinner – which makes life easier when running lots of cables in conduit. So 1km of cable can’t be that expensive surely you’re thinking? Afraid it is! It set us back £700 plus VAT and that was at mates rates!

Paul untangling and reeling the wires (c) John Zabernik

Paul untangling and reeling the wires (c) John Zabernik

However before any of this wire could be installed we had to prepare the cubicle so Tony along with Dan S, Gordon and Connor stripped out all the equipment leaving the just the bare frame of the cubicle looking a bit tatty in all honesty but in good condition structurally. So in stepped John and Sam with their brushes and a tin of rail grey paint. Two coats (and several hours) later it was looking splendid. Very shiny and smart, just a shame it will be tucked away and not on display!

41001s shiny cubicle (c) John Zabernik

41001s shiny cubicle (c) John Zabernik

Tony has now started making excellent progress on putting everything back into the cubicle and the long task of the re-wire. This is one of those tasks that I can’t really update too much on as I’d have to go into detail telling you every single wire thats been put in or which connectors are there so I shall just say progress is good and his excellent work is appreciated by us all and without his hard work we would not be where we are now.

The cab internals have now been reduced to a big hole where the cab instruments on the desk used to be (don’t worry they have just been put aside for tidying up and to make this part easier). Mike has been instrumental to the cab disassembly and has spent hours banging and swearing at errant screws that are rusted solid into the metal work. He has taken the panels away, rubbed them down and repainted them so we now have a nice surface to work with.

A lot of painting has taken place in the power car, mainly to bits of metalwork that were rusting or likely to go rusty. James and Dan have spent a fair amount of time painting the inside of the engine room in red oxide to prevent serious rusting or corrosion. James then followed this by painting a large section of the engine room in battleship grey, once again to tidy it up make it look smart.

One thing we did find on the prototype that isn’t going to work for us is the shaft. The bolts that BR originally used are non-standard and no longer used. So the shaft had one size of bolt and the valenta power unit another sized hole. The obvious result here is the prototype shaft won’t attach onto the vulkan on the power unit. So the only realistic solution for us was to use one of the production shafts from our pool of spares. As the prototype was originally designed to have a V16 engine (requiring a longer shaft) this meant we would need to get our production shaft lengthened. We sent it to GKN who made the necessary adjustments and when it returns it shall fit on both ends nice and snug!

We then moved to test the radiator. To do this we quite simply filled it with water and internally it all held and we had no leaks. There were a few leaks underneath with Dan getting the lucky (and wet) job of diagnosing these. Luckily it was just found that the power car would need a trip over a pit road and a zip gun to really tighten the bolts and prevent leaks.

Dan checking to see where the water was coming from (I think I know where...) (c) James Trebinski

Dan checking to see where the water was coming from (I think I know where…) (c) James Trebinski

You may remember that we took the corridor connection off the back of the powercar as it was in a bad state. We have earmarked one from the EMT buffer car involved in the shunting incident at Neville Hill. EMT have very kindly agreed to fit this for us too.

We’ve managed to sort out all of our filtering too in all areas. The air filters are exactly the same as the production ones so they’ve been acquired and fitted. Both fuel filters have also been changed. The oil filter proved to be a bit of a puzzle though as they are different to those fitted on production power cars. Luckily we found a source for these and they are ready to be installed.

We’ve also managed to acquire free of charge a set of brake pads from Ferodo however after inspection it became apparent that they were the wrong size. Luckily our contact at Ferodo was very understanding and we should hopefully have the correct pads soon.

Once again I won’t apologise for the lengthy update as again it does prove exactly how much we are doing and we like to go into detail for you.

 

Oh what a Knight

Well as 2012 drew to a close we were thrilled to hear that Kenneth Grange, the designer responsible for the look of the HST featured in the Queens New Years Honours list. Sir Kenneth Grange who has been knighted for his services to design was awarded a CBE nearly 30 years ago showing that his excellent design work is being recognised.

Here at Project Miller we are thrilled for Sir Kenneth and especially pleased that he has always heralded the Intercity 125 as his proudest design. We’d like to extend our warmest congratulations to Sir Kenneth and thank him for designing such an iconic train.

This great news brought a great year for us to a close. We are amazed with how much progress we have made thanks to our volunteers, supporters and industry friends. We are sure that 2013 will be even better for us. You can follow our progress here to see how we’re getting on as well as on twitter @41001_PM

Happy new year!

Sir Kenneth Grange next to 41001 (c) John Zabernik

Sir Kenneth Grange next to 41001 (c) John Zabernik

 

Project Miller hitting your screens soon…

We are pleased to announce that a film about Project Miller and the restoration of Prototype Power Car 41001 will be shown on the BBC TV programme ‘INSIDE OUT – YORKSHIRE AND LINCOLNSHIRE’ to be broadcast this coming Monday 26th November on BBC1 from 19:30 to 20:00.  This will include interviews with the 125 Group restoration team and the designer of the HST nosecone Kenneth Grange, filmed during his visit to East Midlands Trains depot at Leeds Neville Hill in September.  This is a regional programme and will only be broadcast on BBC1 in Yorkshire and Lincolnshire however it will also be available for all to watch on the BBC iPlayer from Tuesday 27th November for 7 days, www.bbc.co.uk/iplayer 

Toby Foster being filmed in 41001s engine room for BBC programme Inside Out (c) John Zabernik

My we’ve been busy…

Towards the end of October we posted a brief update on the project and what had been going on. Now its time to go a bit more into detail for you. This is the biggest update yet so get comfy…

So, what have we been up to? Well last time we updated you we reported what a successful event Railfest had been and what a wonderful time we all had. Railfest ending meant we had some serious work to get done. On 22nd June 2012 our good friends from Devon and Cornwall Railways (DCR) turned up with their trusty 31601 (which has hauled all our moves to date) and late afternoon 31601 left York NRM with 41001 in tow heading for Neville Hill Depot, Leeds via Castleford.

On Sunday 24th June arrived and we had Gary and Ben at our storage facility who were preparing everything for the move to Neville Hill. Valenta engine S508 had been prepared and was ready to head to Neville Hill as well as some other bits and bobs such as gaskets, trunking and relays. On Monday morning Gary and Ben once again returned to find the low loader ready and waiting. S508 was loaded onto the low loader ready for its journey to Leeds and left late morning.

Ben and Gary then sorted things, tidied up and left for Leeds to join three other volunteers already there. James, Dan and Chris had been at Neville Hill all day preparing the power car to have S183 and the alternator removed so S508 could be dropped in. S508 arrived at Neville Hill around 16:30 so it was all action stations to remove it off the low loader. With S183 and the alternator out and S508 ready to go in we thought that was a good days work and left it at that.

Tuesday saw Ben, Gary, Chris and James remove the various bits and bobs from S183 that we would need for S508 along with some preparation work on S508. The Vulkan coupling was changed from a Voith type to a Marston type.

Wednesday saw our biggest team yet. We had Ben, James, Tony, Mike, Danny and Gordon. An executive decision was made that the wiring was in a mess in the cubicle with many connections not actually going anywhere thanks to Derby RTCs modifications. Next thing you know the cab wiring has come out (along with many desk panels) but this enabled us to take a better look at that department. While this was going on Mike, Danny and Gordon were round the back of 41001 taking a look at removing the gangway. It put up a fight but it was off and this enabled us to take a look at the state of it. The rusty floor plate needed attention but generally everything else at the back of the power car was looking good. A new gangway will be fitted at a later date. Wednesday ended with the news that 41001 should be in the lift bay for Thursday morning.

When we arrived on Thursday morning we found 41001 in the lift bay, excellent! It got better when an enthusiastic Team Leader called Graeme turned up and asked us what we wanted lifting first. First the exhaust silencer came off followed by the roof panel over the engine bay. Before we knew it we had the Valenta power unit lifting beam on the crane and we were ready to rumble. A quick phone call to the BBC (who are collecting footage from the project for an upcoming TV programme) and they were on their way. Next was to separate the alternator and S183 shortly followed by S508 being joined up to the alternator. What a busy day with lots achieved.

S183 and alternator are removed

S183 and alternator are removed (c) James Trebinski

Friday had come around very quickly we needed S508 in today so lets crack on with the work. Ben and Gary set to work with getting the bolts torqued up on the power unit and alternator. After lunch the lifting team from East Midlands Trains arrived at 41001. A short while later it was hooked up and ready to go! An engine lift is a very delicate and slow operation, almost teasing us as we anticipated the engine and alternator going into the power car. However, at 14:00 hours S508 and the alternator landed on the bedplate and were bolted in. What a week it had been and we all deserved a well earned drink so headed to the pub!

S508 lifted into 41001

S508 lifted into 41001 (c) James Trebinski

Hopefully you’ve read this far but I make no apology for it being this long. We have made such superb progress and I didn’t want to leave any bits out. Many thanks to all that have helped us so far: James Trebinski, Dan Webster, Mike Sawyer, Danny Sladdin, Gordon Ogden, Chris Rose, Tony Shaw, Alex Wood, Gary Heelas and Ben Webber. All are very much valued and appreciated. Forward and Onward!

We recorded the historic moment of S508 being lifted into 41001 – so please watch here.

We’ve had a visitor…

On Wednesday 18th September 2012 Neville Hill was visited by a special guest. The designer Kenneth Grange; responsible for designing the nose cone of the Intercity 125 came to see how progress with Project Miller was going. Kenneth was also joined at Neville Hill by cameras from the BBC who would be gaining material for an upcoming broadcast of the ‘Inside Out’ TV programme. We were thrilled to have this opportunity so on the previous Sunday the Project Miller cleaning team were dispatched to Neville Hill to ensure we could show off the shiny and clean power car to the cameras.

On the Wendesday morning Kenneth and the BBC (featuring radio DJ and comedian Toby Foster) were met by two of our volunteers John and James; who were both found hard at work on 41001. 43055  (recently named ‘The Sheffield Star 125 Years’) had been placed alongside 41001 in the power car bays at Neville Hill to show off East Midlands Trains and to also show the comparison between the two.

The BBC cameras shot plenty of footage of 41001 and an interview with Kenneth. Toby Foster asked Kenneth about the evolution of the nose cone, comparing the two power cars. After this Kenneth was invited for a tour of the depot in 43055 by Neville Hill chief Jon Veitch. Kenneth enthusiastically accepted this invitation so squeezed into 43055′s cab along with Toby Foster, BBC cameraman Phil, Jon Veitch, the driver and the shunter. The tour of the depot finished on the turntable at Neville Hill finishing with a superb spectacle with 43055 on the turntable. Kenneth remarked “I want to own a power car one day and a turntable would be a nice thing to display it on”

Project Miller were thrilled to have Kenneth Grange and the BBC along for the day to see our work and how much we have come on in the past year and a half and we look forward to the broadcast of Inside Out. Of course this website will be the place to find out when it will be broadcast.